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The fun fly was scheduled originally for the 12th, but that day was forecast for very cold and blustery winds over 20 mph and yours truly, the event director, postponed it for one week. Sunday the 19th turned out to be a great flying day considering it was February in South Dakota. Winds were 1-5 and the temps were in the 40’s. You may remember from the last meeting, that this year we are going to
try to spice up the fun flies just a little. We still have a lot of hot
dogs left, so slightly burned hot dogs will be featured at each event
until the dogs run out. Also donuts and other assorted goodies will be
on hand. As an added bonus, I brought a handful of helium balloons to
use in a ribbon cutting event. We tied about 30 feet of crepe paper to
the first couple of balloons and launched them from the south boundary
of the property. They climbed pretty good, but even the light southerly
breeze soon had them out of range to the north. Even so, Zac Roller and
Gene Steeley took quite a few spirited passes toward the streamers before
they floated out of sight. On the second attempt we moved the balloon
release point south about 100 yards into the plowed field. On this attempt,
Darrell Cassidy, Ken Gatzke and Gene Steeley took a whole lot of shots
at the ribbon before it left the area. With his agile profile biplane,
Ken Gatzke probably made the most passes If we do, we may try tethering the balloons somehow. That would make it a more leisurely event and also would reduce the risk of a midair collision. If any of you engineer types can figure out how to tether the balloons so they still have some altitude on a windy day, we need your input. Lots of other flying took place including the maiden flight on Bob Olson’s Saito 100 powered Frenzy. Even with the new motor running very rich, it looks like that airplane is going to be a real sweetheart. As the day progressed, the dogs and donuts were passed out and lots of great flying took place on the warm pre-spring day. The only casualty was my LA Racer. I managed to put it through the fence on take off as I lost elevator control just before lift off. As it turns out the battery was bad and I guess it was lucky I didn’t get it farther into the air. It has since been repaired and awaits our first racing event scheduled in March. |